project89
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well u guys know i was building a 3.0 and had it dynoed well it kinda blew up on the dyno @ 6,200-6,300 rpms and hp was still climbing at that point
481 hp @ 6,200 rpms
438 ftlbs @ 5,300 rpms
these numbers were at 16 psi from a gt45 turbo and are flywheel numbers
aparently one of the intake valves droped and destroyed the head,piston and the #4 cyl
im posting from a cell phone so soon as i can get on from a pc ill post the carnage pics
but plans are to order up a replacement piston, and get a new head and put it back together and then redyno with the s475 turbo @ 21 psi
481 hp @ 6,200 rpms
438 ftlbs @ 5,300 rpms
these numbers were at 16 psi from a gt45 turbo and are flywheel numbers
aparently one of the intake valves droped and destroyed the head,piston and the #4 cyl
im posting from a cell phone so soon as i can get on from a pc ill post the carnage pics
but plans are to order up a replacement piston, and get a new head and put it back together and then redyno with the s475 turbo @ 21 psi
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4 bolt mains, I hope. Either way it would be fun to see a crank blasted through the pan. 

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Pillsbry10
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haha whoops guess its not just hybrids that go boom
...so thats
400hp
373tq
at 15% drivetrain loss
...so thats 400hp
373tq
at 15% drivetrain loss
Ouch man, sorry to hear. Block ok then or will you need another?
Senior Member
I feel cheated it says carnage pics but there really isn't any carnage pics. 
Did you figure out what caused the valve to come loose?

Did you figure out what caused the valve to come loose?
project89
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block is toast, i almost told the shop to ditch the 3.0 and just build me a 3.4 but the 3.0 will deffinatly perform as expected so its going to be rebuilt.
but they are trying to figure out why it droped the valve before the new motor goes together, im suspecting the high spring rate valve springs was the cause as i didnt use anything special for locks and retainers
and also the 1.15 ar hotside is to large motor didnt hit 16 psi till just shy of 6k rpms so the .96 housing on the s475 will help out big time
but they are trying to figure out why it droped the valve before the new motor goes together, im suspecting the high spring rate valve springs was the cause as i didnt use anything special for locks and retainers
and also the 1.15 ar hotside is to large motor didnt hit 16 psi till just shy of 6k rpms so the .96 housing on the s475 will help out big time
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Doom86...
Quote:
Originally Posted by project89
im posting from a cell phone so soon as i can get on from a pc ill post the carnage pics Senior Member
i usually save this comment for girls, but thats redonkulous. any plans for pushin more hp? and gl w/ the rebuild.
project89
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yes im looking for atleast another 120 hp and 100 ftlbs which it should hit with the s475,prolly wont even have to turn the boost up to 21psi, the numbers were still climbing when the valve droped. motor should make peak power in the 7.5-8,200 rpm range
i dont plan on pushing the motor any further then that.as that should be enough power to go low 10's high 9's i may swap to a close ratio manual trans with this engine though
i dont plan on pushing the motor any further then that.as that should be enough power to go low 10's high 9's i may swap to a close ratio manual trans with this engine though
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Quote:
I read that fine the first time. But when I go clicking a link with supposed carnage I want to see some that's all. I had my eyes all ready for some motor guts and didn't get any.Originally Posted by bl85c
Doom86... It's coming, I'm subscribed so it's handled. Thanks for the heads up though.

im disappointed, i dont see any sweet carnage pics!
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Junior Member
thats ridiculous!! i want 480 hp.....
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Well Dave, I don't feel so bad about the first destroked 3.4 being iron headed. It sounds like you put work into it to make it deserving. Too bad it crapped on the dyno. Now pictures!
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I thought this post had car **** also.
I know how you feel I had a 302 Ford I built do that twice on the same motor and build. First it was a bad cam Alliance Cams brand. Almost all of the lobes broke apart. The parts store knew the cam was bad when I took it back because everyone that bought one had the same issue. They never called me to let me know. They replaced it with a new Crane Cam. I pulled the motor apart cleaned everything flushed out all of the oil returns. Rebuilt the motor for the second time that week and it ran for 15 minutes! One of the rod bolts broke and rapped around another rod. It tore the rod out of the piston, the piston was still up top. That was a bad week that week. Third time was the charm different block, crank, rods and pistons. It's still running 14 years later.
I know how you feel I had a 302 Ford I built do that twice on the same motor and build. First it was a bad cam Alliance Cams brand. Almost all of the lobes broke apart. The parts store knew the cam was bad when I took it back because everyone that bought one had the same issue. They never called me to let me know. They replaced it with a new Crane Cam. I pulled the motor apart cleaned everything flushed out all of the oil returns. Rebuilt the motor for the second time that week and it ran for 15 minutes! One of the rod bolts broke and rapped around another rod. It tore the rod out of the piston, the piston was still up top. That was a bad week that week. Third time was the charm different block, crank, rods and pistons. It's still running 14 years later.
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n4carnage
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Bumping this in hopes of carnage soon... 

I want to see pics. also, you know the rules...pics of dyno sheet, too! 

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Quote:
Originally Posted by AM91Camaro_RS
I want to see pics. also, you know the rules...pics of dyno sheet, too!



Supreme Member
I don't think we are badgering him enough. Pictures!!!! Me want pictures!!!!
Supreme Member
Hey, easy guys. He's only had 6 days. 

Senior Member
Well like he said he just moved so give him a few more days to get everything settled cable installed computer unpacked and setup
I'm sure well get the pictures and info soon enough
I'm sure well get the pictures and info soon enough

project89
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sorry guys i got into des moines last sunday and started work on monday, well i havent had a day off since and have been working 10-14 hour shifts so i havent had time to do a thing, soon as i get internet and dont have to use my cell ill have the pics posted
the verdict on the droped valve is that the retianers could just not withstand the spring presures the valve springs had 215# seat presure and around 490#'s open presure, so im going with different retianers and locks this time around, the machine shop is curretly trying to find me a suitable 3.4 block to use the one they did pick up needed to much work to be used
wdit
and actually if i get to pick up my blackberry tommorow i should be able to post pictures
the verdict on the droped valve is that the retianers could just not withstand the spring presures the valve springs had 215# seat presure and around 490#'s open presure, so im going with different retianers and locks this time around, the machine shop is curretly trying to find me a suitable 3.4 block to use the one they did pick up needed to much work to be used
wdit
and actually if i get to pick up my blackberry tommorow i should be able to post pictures
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Quote:
the verdict on the droped valve is that the retianers could just not withstand the spring presures the valve springs had 215# seat presure and around 490#'s open presure, so im going with different retianers and locks this time around, the machine shop is curretly trying to find me a suitable 3.4 block to use the one they did pick up needed to much work to be used
wdit
and actually if i get to pick up my blackberry tommorow i should be able to post pictures
Originally Posted by project89
sorry guys i got into des moines last sunday and started work on monday, well i havent had a day off since and have been working 10-14 hour shifts so i havent had time to do a thing, soon as i get internet and dont have to use my cell ill have the pics posted the verdict on the droped valve is that the retianers could just not withstand the spring presures the valve springs had 215# seat presure and around 490#'s open presure, so im going with different retianers and locks this time around, the machine shop is curretly trying to find me a suitable 3.4 block to use the one they did pick up needed to much work to be used
wdit
and actually if i get to pick up my blackberry tommorow i should be able to post pictures
Damn you are close to me now.. if you happen to be near Davenport at all shoot me a PM.

Senior Member
I can't wait till you get everything worked out and get her back on the dyno
Senior Member
Thats crappy having that happen. I had a pride and joy engine decide to spit a rod out of the side of the block on me once. Talk about miserable. CARNAGE PICS!!!
project89
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Quote:
yes engine dyno with all accesorys hooked upOriginally Posted by firstfirebird
So this was on an engine dyno? project89
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Sorry guys my job bumped me to 16 hour shifts i barley have time to sleep let alone get internet ser vice &d other things done that i need to do. Im working on it though i do have 2? S though first does anyone know of a decent mob ile web browser for a java based phone that will allow uploading of files over the phones web connection.
And number two im thinking i want to replace the rod in the cyl that droped the valve . But the machine shop says the rod is fine.i would think that the valve head getting jammed between the head and piston would put a bit of a buse on the rod what do u guyd think reuse it or replace it for piece of mind
And number two im thinking i want to replace the rod in the cyl that droped the valve . But the machine shop says the rod is fine.i would think that the valve head getting jammed between the head and piston would put a bit of a buse on the rod what do u guyd think reuse it or replace it for piece of mind
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I could PM you my number and you could text me the pictures and I'd upload them for you
Supreme Member
As long as the rod is straight and not cracked it's fine. Put it back in.
Supreme Member
I don't know if you were using the standard 5.7" rods, but if you're really looking to replace that rod, I think I still have the pair of 2.8 rods in the garage with pistons...
Senior Member
hey man..... 20 days and no pics of sexploded engine parts... what gives?!
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Well there's only 11 requests for pictures so far. I think he's holding out for 12.
Supreme Member
^lol
and 16 hour shifts. Damn.... Overtime
and 16 hour shifts. Damn.... Overtime

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16hrs, that's it? I work my day job 7-4 than go to my shop till 12 or 1am M-F and still can manage pics. Someone even offered to host them from the cell pics!
This isn't like the old Daves12secv6 that had "400whp" in his sig a few yers ago and couldn't break 13's, is it?
This isn't like the old Daves12secv6 that had "400whp" in his sig a few yers ago and couldn't break 13's, is it?
Quote:
This isn't like the old Daves12secv6 that had "400whp" in his sig a few yers ago and couldn't break 13's, is it?
Indeed it is, the very same one.Originally Posted by firstfirebird
16hrs, that's it? I work my day job 7-4 than go to my shop till 12 or 1am M-F and still can manage pics. Someone even offered to host them from the cell pics!This isn't like the old Daves12secv6 that had "400whp" in his sig a few yers ago and couldn't break 13's, is it?
Supreme Member
Easy now. We won't get pics if we start arguing...
Quote:
We won't get pictures anyway. Originally Posted by bl85c
Easy now. We won't get pics if we start arguing... 
Supreme Member
Aww you ruined the joke! You were supposed to infer that yourself. He could still take a hammer to a valve and piston though. Pictures! Pictures now!
Member
Quote:
Ok I'll make number 12 then where are the pic's???Originally Posted by bl85c
Well there's only 11 requests for pictures so far. I think he's holding out for 12. Member
Quote:
Originally Posted by Six_Shooter
We won't get pictures anyway

Junior Member
I call shenannigans, no pics after 3 months? You sir, are fired!
Senior Member
dammit! i was hoping there was an update on this....
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Pillsbry10
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Lol no such luck
Member
Quote:
481 hp @ 6,200 rpms
438 ftlbs @ 5,300 rpms
these numbers were at 16 psi from a gt45 turbo and are flywheel numbers
aparently one of the intake valves droped and destroyed the head,piston and the #4 cyl
im posting from a cell phone so soon as i can get on from a pc ill post the carnage pics
but plans are to order up a replacement piston, and get a new head and put it back together and then redyno with the s475 turbo @ 21 psi
Originally Posted by project89
well u guys know i was building a 3.0 and had it dynoed well it kinda blew up on the dyno @ 6,200-6,300 rpms and hp was still climbing at that point481 hp @ 6,200 rpms
438 ftlbs @ 5,300 rpms
these numbers were at 16 psi from a gt45 turbo and are flywheel numbers
aparently one of the intake valves droped and destroyed the head,piston and the #4 cyl
im posting from a cell phone so soon as i can get on from a pc ill post the carnage pics
but plans are to order up a replacement piston, and get a new head and put it back together and then redyno with the s475 turbo @ 21 psi
Thats amazing i didn't think our motors could actually put out those numbers with a single turbo...but with intake valve dropping in like that i believe it was a weak spring...still interesting though





